WE Report

Lessons Learned

Lesson Learned





By: Rob Banbury

Report No.

465

Discipline/Origin

Drilling
No origin

Well

Schweinsteiger
6204/11-3

Date created

2020/08/27
1927 days ago

Project Phase

Operational
Project Phase

LL Type/Classification

Operational
Positive

Borgland Dolphin


What happened in Top hole:
Good suggestion from Dolphin not to do this as in past fibreglass tubing has broken due to vibration and impact on inside of conductor. Also, and more important, safer to keep rig skidded off while RIH pilot hole BHA in case dropped.

What Was Planned

Release 30″ WHH running tool, circulate clean with fibreglass stinger inside conductor, POOH, run pilot hole BHA with rig over well centre.

What Was Learned

Skidded rig 20m off well centre after POOH stinger clear of WHH.

What Actions Are Required

Include this procedure in future DOPs.

EDITOR


CLOSE LL (testing)





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